I could not get the Sik radio to communicate with the FC on UART3. I fully configured my quad with compass and mag. It seems that by fluke only, the Dec 26 version installed and Boot Looping stopped. The Nov 20 version resulted in Boot Looping and each time it happened it would be necessary to fix windows with Zadig and then the ImpulseRC tool. I installed the iNAV firmware from the Matek website (after the versions in the configurator failed with Boot Loops) which offered TWO variants of 2.1.0 at the time. I very recently completed a 250mm Quad build with a Matek F722-SE board and Betaflight 3.5 installed flawlessly. I think this problem in Issue #4076 still persists.
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